■ ■ fill; ■ ■ ■ ■ ■ ■ ■ W& m szJES mUBDaMHSBK ■ 1 ■•\ / - 1 "-" ' "* ^ .A" fro •% f •jflfe'- ^ ^ .'^stok-., -\/ _.^s^.. ^ ^ ( • o' %/?%*' y %^-y x-^-y */?&•' y % - **n< ^ » j -Sb*° ^% F** y%, -.wis- r0 c°" "♦ **<3 ^c q* a.° »l^> ^ v ' ,^ c ' ,+* X ^ • > ^ A. *W^* ^ V % .' ^/ .'Jill; %° ^ , '- •'% ^-^^ o - ^tiifcX ^.^v% /\ ^q* V** i,- V ^ v • I ' 4**X Io WM?*° j?X, j °' ^Ol Bureau of Mines Information Circular/1987 Surface Testing and Evaluation of the Monorail Bridge Conveyor System By Robert J. Evans, William D. Mayercheck, and Joseph L. Saliunas UNITED STATES DEPARTMENT OF THE INTERIOR Information Circular 9146 Surface Testing and Evaluation of the Monorail Bridge Conveyor System By Robert J. Evans, William D. Mayercheck, and Joseph L. Saliunas UNITED STATES DEPARTMENT OF THE INTERIOR Donald Paul Hodel, Secretary BUREAU OF MINES David S. Brown, Acting Director Library of Congress Cataloging in Publication Data: Evans, Robert J. Surface testing and evaluation of the monorail bridge conveyor system. (Information circular ; 9146) Bibliography. Supt. of Docs, no.: 1 28.27: 9146. 1. Mining machinery -Testing. 2. Monorail conveyors -Testing. 1. Mayercheck. William L). II. Saliunas, Joseph L. III. Title. IV. Series: Information circular (United States. Bureau of Mines) ; 9146. TN295.U4 [TN345] 622 s [622'.66] 86-600401 CONTENTS Page Abstract Introduction Background Description of monorail bridge conveyor system 3 Conveyor units • • Power and control 5 Tramming and support system 8 Inby support 9 Outby support 9 Surface testing 10 Test rig installation 10 Initial checkout 11 Power consumption 12 Disabled brake test 14 Haulage rate 14 Miner loading trials 16 Reliability 17 System compatibility with low-belt structure 20 Suspension of monorail track by chain hangers 20 System compatibility with hopper-feeder 22 Summary of surface test findings 22 Modifications 22 Mining plans 24 Conclusions 31 Appendix A. — Modifications to the monorail bridge conveyor system 32 ILLUSTRATIONS 1. Three types of monorail bridge conveyor units 3 2. Plan view of monorail bridge conveyor unit 5 3. Intermediate unit 6 4. Inby unit 6 5. Outby control boxes 7 6. Pendant control 7 7. Monorail T-section track configurations 8 8. Monorail hardware 9 9. Outby support with dolly 10 10. Surface test rig 11 11. Monorail bridge conveyor system in test rig 11 12. Typical power-consumption plots 14 13. Closed-loop configuration 14 14. Monorail bridge conveyor units at maximum-angle relationship 15 15. Haulage-rate plot 16 16. Haulage-rate and power plots during maximum haulage-rate trial 16 17. Continuous miner loading directly into monorail bridge conveyor 17 18. Loading rate and power consumption during reliability trial 18 19. Spillage under inby monorail bridge conveyor transfer point 19 20. Profile of chain-suspended monorail track 21 21. Chain hanger 21 22. Hopper-feeder-bolter 23 23. Hopper-feeder-bolter compatibility trial 23 11 ILLUSTRATIONS— Continued Page 24. 25. 26. 27, 28. 29. 30. 31. 32, 33. 34. 35. 36. Monorail installation with chain hangers , Monorail installation with roof plates over low-belt structure. Monorail bridge conveyor track turnout plans , Five-entry mine plan Five-entry 60° mine plan with rooms , Seven-entry mine plan , Mine plan for longwall panel-entry development , Monorail bridge conveyor used with shortwall mining system...., Monorail bridge conveyor with continuous miner , Hopper-feeder-bolter , Monorail bridge conveyor used with hopper-feeder , Monorail bridge conveyor-hopper-feeder interface , Monorail track, installation plan , TABLES Monorail bridge conveyor specifications , Monorail bridge conveyor power consumption , 24 25 25 26 27 27 28 28 29 29 30 30 31 4 13 UNIT OF MEASURE ABBREVIATIONS USED IN THIS REPORT ft foot lb/ft pound per foot ff lb foot pound min minute ft/min foot per minute pet percent h hour r/min revolution per minute hp horsepower s second Hz hertz St short ton in inch st/h short ton per hour in/ft inch per foot V ac volt, alternating current kW kilowatt V dc volt, direct current lb pound W watt SURFACE TESTING AND EVALUATION OF THE MONORAIL BRIDGE CONVEYOR SYSTEM By Robert J. Evans, 1 William D. Mayercheck, 2 and Joseph L. Saliunas 3 ABSTRACT The monorail bridge conveyor (MBC) is a prototype continuous face haulage system that was surface tested and evaluated by the Bureau of Mines. The MBC consists of a series of cascading belt bridge conveyors suspended from roof-supported monorail track. Tests were conducted to determine MBC haulage capability, maneuverability, power consumption, and reliability using rigid and chain-suspended monorail track installa- tions. Subsequent modifications to improve operation and reliability made during surface testing are described. Mining plans were devised to show potential MBC installations for room-and-pillar, longwall devel- opment, and shortwall mining sections. Compatibility tests were con- ducted with the Bureau's prototype hopper-feeder, to provide additional surge capacity and lump-breaking capability. Results from the surface test program, along with modifications to improve system operation and reliability, indicate that the MBC has the potential to perform success- fully in an in-mine trial. 'Civil engineer, Pittsburgh Research Center, Bureau of Mines, Pittsburgh, PA. Supervisory physical scientist, Pittsburgh Research Center. 3 Project engineer, Boeing Services International, Pittsburgh, PA. INTRODUCTION The Bureau of Mines has sponsored nu- merous high-risk research programs over the past decade to improve productivity and health and safety in underground coal raining by advancing state-of-the-art con- tinuous face haulage systems. These sys- tems are designed to move coal nonstop from the continuous miner to the next stage of rail or belt haulage (approxi- mately 500 ft). One of the more innova- tive continuous face haulage systems is the monorail bridge conveyor (MBC). The MBC consists of a series of cascading belt conveyors supported by an inverted T-section monorail bolted to the mine roof. The basic concept was conceived and patented by the Bureau in 1979 (U.S. Pat. 4,157,757). It was designed and fabricated by the Goodman Conveyor Co. , Inc. under a cost-sharing arrangement with the Bureau (contract J0333917). This system has the potential to improve productivity over conventional shuttle- car haulage systems by eliminating shuttle-car change, which can amount to 10 pet of the total face time for a con- tinuous miner per shift; it provides a captive guidance system that requires only one operator, regardless of length; and it allows haulage in poor bottom con- ditions where conventional rubber tired and cat systems could not operate effi- ciently. Two of the MBC safety features are elimination of potential shuttle-car trailing cable and moving-vehicle acci- dents. MBC applications include all room-and-pillar operations such as driv- ing rooms, entries and panels, pillar ex- traction, and shortwall mining. BACKGROUND Underground continuous haulage systems have been employed in Europe and the United States since 1970. Commercially available systems can be grouped into three general categories: (1) crawler- mounted alternating series of mobile bridge carriers and piggyback bridge con- veyors, and (2) monorail suspended sys- tems, and (3) noncascading systems. The crawler-mounted systems generally require an operator every 50 ft and are limited to a total length of under 200 ft. The only commercial monorail system available today has been installed in a U.S. trona mine and at several foreign locations. Although it has a unique con- tinuous belt with no crossover points, it is relatively heavier and more expensive, and it is more difficult to change the system length in comparison with the MBC system, which can attain a length of more than 500 ft with just a single operator. The noncascading systems, which have been recently introduced and remain un- tested underground, are relatively more expensive and present more difficulties in changing the system length. Extensive surface testing and evalu- ation of the MBC was conducted by the Bureau. The objectives of the surface test and evaluation program were to — 1. Rigorously test the MBC and improve performance, based upon observations made under simulated underground operation; 2. Measure MBC performance criteria so that underground performance and operat- ing requirements could be predicted; 3. Determine if the MBC meets its de- sign criteria and is worthy of an in-mine trial; and 4. Prepare the MBC for an in-mine trial including electrical approval by the Mine Safety and Health Administration (MSHA). The principal advantages of surface testing, prior to an in-mine trial, are that equipment performance can be proven, and improved upon, without interfering with production at an operating mine. This is absolutely paramount with face equipment such as the MBC. Even though the MBC has several potential advantages, most mines would not risk the instal- lation and operation of unproven face equipment, since any failure would result in higher operating costs and lost pro- duction. Therefore, the raining industry tends to resist the introduction of novel raining systems if the in-mine trial does not meet anticipated short-term results. Even though the most rigorous surface test and evaluation program will not sub- ject equipment to all of the harsh condi- tions found in underground mines, a sur- face test program does significantly increase the probability that the initial underground trial will be successful. Surface testing of the MBC commenced in September 1982 and final modifications to prepare the MBC for in-mine use were com- pleted in August 1985. DESCRIPTION OF MONORAIL BRIDGE CONVEYOR SYSTEM The MBC consists of a series of cascad- ing belt conveyors suspended from special roof-supported monorail. The MBC-systera specifications are shown in table 1. The three types of MBC units (inby, intermediate, and outby) are shown in figure 1. Each unit consists of a belt conveyor mounted on a rigid frame, mono- rail-suspension hardware, a monorail- mounted tram unit, and electric power and control components. All MBC units are totally monorail suspended except for the inby and outby units. The inby end of the inby unit is mounted on rubber tires, which are steered remotely. The outby end of the outby unit can be supported either by a dolly mounted on a rigid-belt structure or by monorail directly over the section belt. See table 1 for de- scriptions of various MBC components (in- cluding modifications made during the test program). CONVEYOR UNITS Individual conveyor units are fabri- cated from hollow structural tubing, pro- viding a lightweight and rigid frame. Conveyor units are 27 ft, 7 in long over- all, with an active length of 24 ft. Presently, 12 conveyor units are avail- able for a system length of 288 ft; wm/m/Mmmm/mmm//mMW//mf//m/m///im//m j ggjrts^fe-— ^&^^^4&^ m^ Inby unit - — --■ T T --" Intermediate unit Outby unit FIGURE 1.— Three types of monorail bridge conveyor units. TABLE 1. - Monorail bridge conveyor specifications (Prototype system: 12 conveyor units available for 288-ft length; expandable to greater length) .1.2 System specifications Haulage rate, nominal st/h.. 600 Tram speed, constant ft/min. . 60 Electric power requirements, V ac: Main system 460 Control system 120 Power output, total (for 12 units), hp: Conveying 120 Tramming 20 Entry width, recommended minimum f t. . 14 Load, typical maximum on a suspension point lb.. 2,000 Working height, minimum, in: Without low-belt structure 48 With low-belt structure 54 Gradability, recommended maximum pet.. 6.5 Curved-track radius f t. . 24 Crosscut geometry 3 °. . 60-90 Individual bridge specifications: Dimensions, ft: Length: Overall 27.6 Active 24 Width, overall Carrier idlers (on 25° angle), diameter in.. 4 Rollers, head and tail, diameter in. . Belt width in. . 36 Belt speed, constant ft/min. . 400 Power output, hp: Tram drive motor 1.5 Conveyor motor 10 Weight (empty) lb. . 4, 200 Monorail track: 24-ft radius, designed for 60° crosscuts; available in 7- and 10- ft lengths; weight, 7 lb/ft; suspended on 4-ft centers. Inby support: remotely steered rubber tires. 3 90° crosscut: Compound curve must be used with the stipulation that intersecting arc lengths must not exceed 30° to prevent interference. NOTE. — All units can be controlled by single operator; helper optional. Safety features: Belt slip and sequence switches, disk brakes on each tram unit that engage automatically when tram power is shut off, emergency stop on each unit, pendant con- trol from any unit, end-of-monorail stop on inby unit, and warning horn before belt startup. however, with electrical modification, additional units can be added to provide increased system length. A plan view of a typical intermediate unit is shown in figure 2. A 36-in-wide, 5/16-in-thick belt is supported on a conveyor unit with a maximum width of 7 ft. Catenary-type, 4-in-diam carrier idlers are installed on a 25° troughing angle. A 1,750-r/min, 10-hp electric motor powers the belt on each unit. A 7:1 double-reduction gear- speed reducer is coupled to the head- drive roller to provide a constant 400- ft/min belt speed, and 7-in-diam crowned drive and idler rollers are used. The tail idler roller is mounted on an ad- justable screw-type takeup. The belt has a rated capacity of 600 st/h. Compres- sion-spring belt cleaners are mounted under the head roller of each unit. POWER AND CONTROL The MBC is operated by 460-V ac, three- phase, 60-Hz electric power provided by a No. 2/0 trailing cable to the outby main breaker box. Transformers located in each motor control box supply 120-V ac, single-phase, 60-Hz power for the control system. The 10-hp, 440-V ac, single- speed conveyor motors and the 1-1/2-hp, 440-V ac, single-speed, reversing tram motors have across-the-line starting. The motor control box on each unit is equipped with an emergency-stop pushbut- ton station that disengages the main cir- cuit breaker. The electrical system is modular in de- sign with identical power and control wiring on all but the inby and outby units. Figure 3 shows a typical interme- diate unit containing the motor control case and interconnecting cables common to all units. The inby unit has an addi- tional control case (fig. 4) that is required for the steering motor and head- light controls. The outby unit is con- nected to two additional control cases (fig. 5): the main breaker case, which houses the main-system circuit breaker, and the master control case, which con- tains the emergency-stop controls for the entire system. Tail roller Belt sequence switch switch Motor control case J i Head roller Belt takeup mechanism Troughing idler \ Coupler IO-hp electric motor Gear-speed reducer •*- Inby Note: Belting not shown Outby FIGURE 2.— Plan view of monorail bridge conveyor unit. FIGURE 3.— Intermediate unit. FIGURE 4.— Inby unit. FIGURE 5.— Outby control boxes. FIGURE 6.— Pendant control. The MBC system employs automatic se- quential belt startup. When the conveyor is first activated, an audible warning signal is heard. After a brief period che signal stops, and the conveyors start in sequence beginning with the outby unit. Sequence switches allow each suc- cessive unit to start only after the pre- ceding unit is running at full speed. Should a conveyor stop for any reason, all conveyors inby the defective unit will stop automatically. Each unit has a manual ovverride that will operate the conveyor on that unit. This control is intended for maintenance and diagnostic use only. Controls for steering, tramming, and conveying are located on an umbilical pendant control. The pendant control (fig. 6) may be connected to any unit in the system. This provides operator con- venience and allows positioning to avoid blind or unsafe MBC operation locations. During face operations, the pendant con- trol will typically be located on the inby unit, so the operator can best con- trol the inby steering. The MBC system can be trammed on the monorail track in both the inby and outby directions, with each tram motor equipped with an electric brake. The brake re- mains set when the machine is stationary. Upon activation of the tram control, the brake releases and sets again when the tram control is deactivated. If a brake becomes overheated, it can be manually released to prevent further heat buildup. Should any unit develop a major mal- function requiring it to be removed from the system, all electrical connections can be disconnected at the plugs and re- ceptacles that interconnect the units. The units are reconnected in the same manner. TRAMMING AND SUPPORT SYSTEM Both ends of each conveyor unit are supported by eight-wheeL carrier assem- blies that distribute the weight of each conveyor on the monorail track. The carriers are designed to follow both vertical and horizontal curves in mono- rail track without affecting conveyor suspension. A 1,100-r/min, 440-V ac, 1.5-hp traction motor is used for tramming each conveyor unit. The motor drives two rubber wheels that are held against the underside of the monorail track. A 24:1 triple-reduction speed re- ducer is used to provide a constant tram- ming speed of 60 ft/min. Disk brakes on each tram motor automatically engage when the system is not being trammed. Lightweight monorail track is used to suspend the MBC system. The inverted T-section track, made by Cleveland Tram- rail (Cleveland Crane and Engineering, Div. of McNeil Corp., Wickliffe, OH) 4 weighs 7 lb/ft and comes in eight fac- tory-available configurations, as illus- trated in figure 7. Straight rail is available in 14-, 10-, and 7-ft lengths. Curved and combination rails in vari- ous lengths make 60° turnouts with a 24- ft radius. Other lengths and config- urations of monorail can be fabricated underground to suit particular mine con- ditions. A hydraulic rail bender is com- mercially available for field-fitting curves. Four bolts are used to join ^Reference to specific products does not imply endorsement by the Bureau of Mines. 14' , u LH switch 10' I r 7' L MK-I MK-2 NIK-6 MK-3 MK-5 MK-4 straight straight straight curved curved curved Note: All curves on 24-ft radius FIGURE 7.— Monorail T-section track configurations with designated identification numbers. monorail track at overlapping splice plates. Both right- and left-hand man- ually operated monorail switches are available. Figure 8 shows two types of hardware that can be used to suspend monorail track. One type of suspension hardware uses a semirigid connection to suspend monorail track from roof plates attached to the mine roof with two roof bolts. Bevel-headed bolts seated in the roof plates are connected to the monorail track, allowing limited horizontal track movement. A second type of suspension hardware enables a nonrigid connection to suspend the monorail track using a chain- hanger bracket attached to the mine roof with one roof bolt. Varying lengths of chain connect the monorail track to the chain-hanger bracket, allowing horizontal and vertical movement of the monorail track. INBY SUPPORT The inby end of the MBC system is sup- ported by two 9-in-wide rubber tires installed on 38-in centers. The wheels are powered by a 1.5-hp electric motor at 60-ft/min constant tram speed. The tram motor and gear-speed reducer are mounted behind the rubber wheels. A sep- arate 440-V ac, 1.5-hp electric motor and ball thread are used to steer the inby wheel carriage. The steering motor is controlled from the pendant control. The height of the inby conveyor unit over the rubber tires is 32 in. The height was increased to 40 in with the addition of a low-profile hopper. OUTBY SUPPORT In low-coal applications, the monorail track can be offset from the panel belt, and the outby end of the MBC can be sup- ported by a dolly mounted on rigid belt structure (fig. 9) or on a chain panline. The dolly ensures transfer onto the panel belt without spillage. In higher coal, the outby end of the MBC could be sus- pended from monorail installed directly over the panel belt. Chain-hanger assembly Roof plat© FIGURE 8.— Monorail hardware. 10 FIGURE 9.— Outby support with dolly. SURFACE TESTING Surface tests were conducted to verify and measure MBC haulage capability, ma- neuverability, power consumption, and re- liability. Both rigid- and chain-sus- pended monorail track installations were evaluated. Numerous modifications were made to several MBC subsystems to correct deficiencies noted during surface test- ing. Important test sequences were re- corded on videotape and are available at the Pittsburgh Research Center. TEST RIG INSTALLATION A steel structure was constructed at the test facility to support the MBC dur- ing surface testing. This test rig (fig. 10) functioned as a false mine roof and was required to suspend the monorail track. The test rig enabled MBC testing on straight and radius tracks, through switches, and on a 6-1/2-pct grade. It consisted of nine arches that supported underhung beams. Two separate 140-ft lengths of monorail track were supported from the underhung beams. The two mono- rail track sections were parallel to each other and offset by 8 ft. Two 80-ft por- tions of both monorail tracks were in- stalled on a 6-1/2-pct slope. A single, 60-ft arc length of the 24-ft-radius monorail track was connected to the main track by a switch. This basic test rig was used to support both rigidly bolted and chain-suspended monorail tracks. For initial test sequences, the monorail track was bolted to roof plates that were rigidly bolted to the underhung beams. A 140 ft length of auxiliary belt structure was installed under one of the monorail tracks. The belt structure sup- ported a 48-in-wide conventional belt that operated at 625 ft/min and was pow- ered by a 50-hp electric motor. This auxiliary belt was used during closed- loop coal conveying tests. A beltscale weigh bridge was installed in this auxil- iary belt to measure the MBC haulage rate. 11 Offset track t _ Main track 200 2 K -C < O ^ 800 I- 2 «/> p 3 "i — i — i — | — i — i — i — t Adding coai- t — i — r— i — i — r -i—\ — r TZ j^/amJHV *^ |l^f^7^ > *^^*^^**H*Mw4*<'^M>i*y w * l ^i 400 0t i i i i I i_i J I l_l I l_l I I L J I I I l__L 20 -i — i — i — r J ■ ■ ■ i, 25 15 TIME, s FIGURE 16.— Haulage rate and power plots during maximum haulage-rate trial. 30 average of 450 st/h of coal was handled without experiencing problems with the MBC system. The decreasing haulage rate, after coal addition was stopped, was due to spillage at the shuttle car. Spill- age at the MBC transfer points was negligible. A second test was conducted to estab- lish the maximum haulage rate of the MBC system. Belt-motor power consumption was monitored during this test, in addition to haulage rate. Coal was added to the closed-loop circuit until failure of the flat auxiliary belt precluded additional loading. The peak instantaneous loading rate during this trial was 600 st/h (fig. 16). No problems were observed with the MBC system during peak loading rates. All belts remained in alignment, and spillage at the transfer points was mini- mal. The maximum observed conveyor-motor power consumption was 16.8 kW for three motors. These tests verified that the MBC is capable of haulage at its design specification of 600 st/h. MINER LOADING TRIALS The objective of the miner loading tri- als was to verify the ability of the MBC to simultaneously tram and receive coal from the discharge boom of a continuous miner, as would be done underground. A Joy 16CM continuous miner was used to load directly into the hopper of the inby unit (fig. 17). The miner had a 24-in- wide and 8-in-deep chain conveyor area. A 15-st pile of wetted ROM bituminous coal was placed in front of the contin- uous miner. The continuous miner was positioned inby the MBC system, which was located in the radius portion of the test rig. The outby MBC unit discharged onto the 48-in auxiliary belt. A 10-st 17 FIGURE 17.— Continuous miner loading directly into monorail bridge conveyor. capacity shuttle car was used to receive coal discharged from the auxiliary belt. For each trial, the instantaneous load- ing-rate instrumentation was started, the miner was trammed into the coal pile, and the miner operator directed the miner tail boom toward the MBC hopper. The MBC operator, located beside the inby MBC motor-control case, trammed and steered the MBC system as required to locate the MBC hopper under the discharge from the continuous miner. The miner advanced ap- proximately 15 ft into the coal pile un- til the pile was eliminated. After each trial, the MBC and miner were backed up, and the shuttle car dumped the coal in front of the continuous miner. For sev- eral trials, the miner was maneuvered to simulate coal face cleanup operations. Total tonnage for each trial was deter- mined from the belt-scale totalizer. The total tonnage loaded and maximum instan- taneous MBC haulage rate for each trial were: Trial A - 10.1 st loaded at a maximum rate of 690 st/h. Trial B - 8.2 st loaded at a maximum rate of 720 st/h. Trial C - 12.9 st at a maximum rate of 720 st/h. Trial D - 10.0 st loaded at a maximum rate of 630 st/h. Trial E - 7.6 st loaded at a maximum rate of 660 st/h. The miner operator had no problems keeping the inby hopper of the MBC under the miner tail boom as the miner trammed into the coal pile. The MBC operator was also able to maneuver behind the mine during face cleanup operations. This test sequence verified the ability of the MBC to simultaneously convey coal and tram. RELIABILITY To determine the reliability of the conveyor portion of the MBC system, the MBC was installed in a stationary 18 closed-loop configuration. ROM bitumi- nous coal was added to the circuit by slow discharges from a 500-lb capacity loader bucket into the hopper of the inby unit. Coal continued to be added until the belt-scale output showed an average rate of 500 st/h. Recharges of coal were occasionally necessary when spillage losses in the circuit caused the rate to fall to 300 st/h. All coal was wetted prior to loading for dust control. For the entire trial, the instantaneous loading rate, the 48-in auxiliary belt speed, the belt-scale load-cell output, and the total MBC power consumption were plotted on a strip-chart recorder. Dur- ing the reliability trial, an event log was maintained. Event description, time, MBC conveyor hourmeter and totalizer readings were recorded for each test event. Water was applied to the under- side of each MBC belt every hour to con- trol dust generation. During the reliability trial, the MBC conveyors loaded 2,141 st of ROM coal during 5.7 h, for an average loading rate of 375 st/h. Loading-rate peaks of 600 st/h occurred several times during the trial. One failure occurred at 1.3 h into the trial: The conveyor drive cou- pler on the inby MBC unit came apart while the system was hauling at 400 st/h. To repair the coupler, the conveyor drive assembly was realigned with respect to the head drive shaft, and the coupler was replaced. The repair was accomplished by two mechanics in approximately 2 h. One adjustment was necessary at 4.1 h into the trial because it was observed that the outby unit belt was misaligned by several inches. The belt takeup was quickly adjusted without interfering with coal haulage. Figure 18 shows two 36-min, instantane- ous loading rate, and total MBC power- consumption traces. The upper trace oc- curred at 3. 1 h into the trial. After coal addition stopped, the average load- ing rate was approximately 390 st/h. The average power consumption for the same V) 111 5 t- 1,200 |- w a: 900 600 300 V) Z -J O ■£ or 24 20 -1 — r — 1 — 1 — 1 — 1 — 1 — r — 1 — 1 — 1 — 1 — 1 — r— 1 — 1 — 1 — r — 1 — 1 — 1 — 1 — 1 — 1 — 1 — 1 — 1 — 1 — 1 — 1 — p — 1 — 1 — 1 — 1 — r »■• Adding coal »h lL U U « *»44.J' UM t» U * M i 1 — 1 1 1 1 1 1 i_i 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 — 1 1 »- 2 ~ ,„« z-<" 300 2« 2 -J Adding coa JL_JL L _L i. LJ. ±. J Lll J I L-J_ 1 I 1 ■ ' ■ 1 I I 1 I I I I I l_J L TRIAL B TIME-^ Eg 24 20 - 16 - HO (/> CD 2 5 O o TT-T 1 rn r 1 1 1 1 i 1 1 "t 1 i 1 1 1 1 1 1 1 t , Sequence switch opened during trial &£§* 12 --tfy^v^^^^" ■■ -L^ ■ 1 'I ' i ' 1 1 ' 1 ' 1 ' 1 ' ■ 1 ■ J I I I L J I I I I I 1 I I I I I 1 1 1 I 1 l_ TRIAL B TIME CHART SPEED= O.lmm/s FIGURE 18. — Loading rate and power consumption during reliability trial. 19 time was approximately 11 kW or approxi- mately 15 hp; i.e., half the rated motor capacity of 30 hp. The scattered peaks and variations in power consumption were probably due to very fast openings and closings of one or more of the belt-slip centrifugal switches, which in turn shut the conveyor belt motors on and off. MBC belt-speed variations were not noticed during power-consumption variations. The bottom trace was acquired at 4.1 h into the trial when the system was being restarted after a lunch break. After coal addition stopped, the average load- ing rate was 480 st/h. The average power consumption for the same time was 12.5 kW. Observed variations in both total MBC power consumption and loading rate were dampened with time because of more equal distribution of coal in the cir- cuit. Midway through the bottom trace, a belt-slip switch was opened while the left was being cleaned. The belt clean- ers at that time were tensioned against the return belt by a counter-weight of a lever arm. By pulling the lever arm, ex- tra force could be applied to the belt cleaner. In this instance, extra force applied to the belt cleaner caused the return belt to raise and lose contact with the slip-switch roller. After these trials, the counterweighted belt cleaners were replaced with a compression-spring tensioner device. The reliability trial was terminated at 5.7 h into the trial because of a spill at the intermediate discharge point that was caused by excessive coal flow, which buckled the hoop-type deflector. Coal was being added to the system at the time, and the haulage rate exceeded 600 st/h. This spill contributed greatly to the total spillage amount that had accu- mulated at the inby discharge point. Af- ter the trial, spillage at both the inby and intermediate transfer points was raised. There was 700 lb of spillage un- der the inby transfer point, and 4,650 lb of spillage under the intermediate trans- fer point. Figure 19 shows the spillage under the inby transfer point. Prior to the spill, it was observed that spillage under the intermediate transfer point was twice the amount under the inby transfer FIGURE 19.— Spillage under inby monorail bridge conveyor transfer point. 20 point, or approximately 1,400 lb. Based on the lower prespill assumed value, 2,100 lb of spillage occurred during the trial, and the total amount of coal loaded was 2,141 st. Spillage rate dur- ing this trial can then be computed as 0.05 pet of throughput. It is likely that the spillage rate might be higher during in-mine operation, since the sys- tem would be occasionally tramming during conveying operations. During the entire reliability trial, the inby and interme- diate conveyors were at a 5° angle to each other, and the intermediate and outby conveyors were at 20° angles. Dur- ing previous trials, it was observed that the amount of spillage at transfer points increased rapidly as the angle between the conveyor increased. After the tests, the center of the hoop-type deflector was bolted to the suspension frame to prevent future buckling. SYSTEM COMPATIBILITY WITH LOW-BELT STRUCTURE There are several ways that the outby end of the MBC can be located to ensure smooth coal transfer onto the section belt: One way is to suspend the outby unit from the monorail installed di- rectly over the section belt, and another is to attach the outby end of the outby unit to a dolly supported by a low-belt structure. To demonstrate the compatibility of the MBC system with a commercially available low-belt structure, a 32-ft-long section of low-belt structure and a dolly were installed under the chain-suspended right monorail track (fig. 9). The frame of the low-belt structure, designed for use with a 42-in-wide belt, was made of in- terlocking roller assemblies and connect- ing members. The low-belt structure was extended to a total length of 32 ft by the addition of framework made of 5—1/2— in-wide channel sections. Rollers on the bottom and cams on the side of the mating dolly allowed easy mobility on the frame of the low-belt structure. The low-belt dolly was modified by adding an attach- ment bracket. This bracket firmly at- tached the outby MBC unit to the low-belt dolly, while permitting the outby unit to pivot in both horizontal and vertical directions. A 42-in-long drawbar was at- tached between the tram outby motor and dolly bracket. The main power cable to the MBC was then attached to the strain- relief clamp of the low-belt dolly, so that the power cable would always move with the system. No problems were observed as the en- tire MBC system and dolly were repeatedly trammed along the 32-ft, low-belt struc- ture in the inby and outby directions. The dolly moved smoothly on the low-belt structure; the only jerking motion oc- curred during starting and stopping be- cause the outby tram motor was not rigid- ly attached to the outby MBC unit. When the system started tramming, force from the outby tram motor pushing against the drawbar tended to briefly lift the outby motor and suspended monorail track. How- ever, steady-state tramming motion was quickly reached within 2 s because all tram motors were operated at the same speed. The material-handling capability of the dolly-mounted MBC system was not tested. It is expected that transfer of material from the outby MBC unit to the panel belt would not be a problem in a dolly-mounted configuration, since the dolly fixes the outby unit at a constant height from the panel belt, and skirt boards can be added to the dolly as required. SUSPENSION OF MONORAIL TRACK BY CHAIN HANGERS There are several ways of installing special monorail track from the mine roof: One is to rigidly attach the track to roof plates anchored to the mine roof. Another method is to chain-suspend the monorail track from chain-hanger brackets anchored to the mine roof. Roof plates minimize the head room required for sus- pension hardware, but they are difficult to adjust and require two roof bolts. Chain hangers allow easy height adjust- ment and require only one roof bolt, but require extra head room. Initial test sequences were performed with the monorail track rigidly attached to roof plates. To determine if the MBC system could tram on freely suspended monorail 21 Chain FIGURE 20.— Profile of chain-suspended monorail track. FIGURE 21.— Chain hanger. rail track, a 50-ft section of the right monorail track was suspended from chain hangers (fig. 20). To suspend the mono- rail track, chain-hanger assemblies, us- ing various-length, 1/4-in high-strength alloy steel chain with attachment hard- ware, were hung from the roof -bolt mount- ing plates on 4-ft centers. Each chain was held to the simulated mine roof by a chain-hanger bracket, which permitted adjustable chain height. The chain was connected to the top of the monorail track by a 1/2-in hex bolt welded to a chain clevis (fig. 21). A hydraulically powered rail bender was utilized to make concave and convex vertical curves in the inverted T-section monorail track. The rail bender was op- erated by clamping a section of monorail track between a load ram and two pivot points. The load ram was activated by means of a hydraulic handpump. By us- ing a displacement indicator on the rail bender, specific angles could be made in the track. The radius of the bend could be controlled by changing the distance between the load ram and pivot points. The rail bender was then used to install two convex bends of 3.7°, 32 in apart, on the first 7-ft-long monorail track sec- tion. This track section, previously on a 6-1/2-pct upward grade, was bent to end with a 6-1/2-pct downward grade. Addi- tional track sections were then connected to give the track a straight 6-1/2-pct downgrade. When the top of the track reached a height of 68 in from the ground, a single concave bend was made so that the end segment of the track was parallel to the ground. In all cases, each 7-ft-long track section was sus- pended from the support structure by chain hangers on 4-ft centers before the next track section was connected. After the entire 50-ft section of track was suspended, several of the chain-hanger lengths required adjustment to prevent slack in the hanger assembly. The height was adjusted by changing the chain link in the adjustable hanging bracket. To constrain sideways movement, 1/4-in chain installed perpendicular to the monorail tracks was used at the outby end of the suspended monorail track. After the 50-ft segment of monorail track was suspended, the outby end of the outby MBC unit was mounted on a low- belt dolly, as described in the previous 22 section. The ability of the MBC system to tram on chain-suspended monorail track was then observed. No problems were experienced as the dolly-mounted MBC system was repeatedly trammed in both the inby and outby di- rections on the chain-suspended mono- rail track. The eight-wheel carrier as- semblies negotiated a 13-pct change in grade over a 3-ft distance without any noticeable binding. Sideways movement of the suspended monorail track was not observed. SYSTEM COMPATIBILITY WITH HOPPER-FEEDER Although the inby MBC unit can be loaded directly by a continuous miner, in most cases, it would be desirable to In- clude surge and breaker capabilities be- tween the miner and the MBC. The Bureau has developed a separate prototype mining machine, the hopper-feeder-bolter (HFB), to perform that task. The HFB is a cat- mounted vehicle that includes a 5-st ca- pacity surge hopper, an onboard lump breaker, a variable-angle discharge boom and an optional bolter-module (fig. 22) to permit bolting beside a two-pass con- tinuous miner. This provides the advan- tage of eliminating face-to-face place changes during the mining cycle. The bolter module was removed and only the hopper-feeder (HF) was used during trials with the MBC. To evaluate the ability of the HF to load the MBC, a compatibility trial was conducted. The HF was located inby the MBC, and the MBC was loaded with coal discharged from the HF. The low-profile hopper on the MBC was removed to enable the 16-in profile HF discharge boom to fit between the top of the inby MBC unit (32 in) and the underside of the monorail track (59 in). As shown in figure 23, there was little clearance between the HF boom and the top of the inby MBC unit and a very small target area on the MBC to permit loading without spillage. During the loading trial, the MBC was able to haul all coal being discharged at the maximum HF loading rate; however, exces- sive spillage was observed at the trans- fer point between units. An improved in- terface between units would be required before they could be used together. Since the HF boom must clear the under- side of the monorail track, the exact de- sign of the interface will depend upon the height of the monorail installation at the mine site. SUMMARY OF SURFACE TEST FINDINGS Surface testing verified that the MBC system properly performs its design func- tions and is worthy of an in-mine trial. Hightlights of the surface test program are summarized below. power consumption was several tram-motor • Tram-motor measured for configurations. • The braking system is more than ade- quate, as one functioning brake unit held three loaded MBC units on a 6-1/2-pct grade. • The ability to haul the design ca- pacity of 600 st/h was verified. • The MBC was capable of being loaded by a continuous miner. A maximum haulage rate of 720 st/h was measured during the miner loading trials. • During a reliability trial, the MBC system loaded 2,141 st of coal in 5.7 h with only one minor coupler failure. • The MBC was trammed with the outby end supported by a dolly mounted on a low-belt structure. • The MBC was able to tram from mono- rail suspended from roof plates and chain hangers. • The MBC is compatible with the HF, which provides surge capacity and lump- breaking capability inby the MBC. An im- proved interface between the MBC and HFB is required to suit mine conditions. MODIFICATIONS Numerous modifications were made to the original system design to correct the problems observed during surface testing. A complete listing of modifications is contained in appendix A. Major modifica- tions included. 23 *sa^ FIGURE 22.— Hopper-feeder-bolter. FIGURE 23.— Hopper- feeder compatibility trial. 24 • Conveyor belt head and tail rollers were crowned to improve belt tracking. • The clearance area in suspension frames was increased to create more area for coal transfer between conveyors. • Deflectors to direct coal flow and control spillage were installed at con- veyor transfer points; belt cleaners were installed on the underside of each conveyor. • Remote-controlled steering was installed. • A limit switch to prevent the system from tramming at the end of the monorail was installed. • A lightweight pendant control was installed. • The wheel base of the inby wheels was increased for greater stability. • The control circuitry was changed to utilize an intrinsically safe control pendant. MINING The review process for the MSHA experi- mental permit was initiated in December 1984. Review of the control circuitry revealed some problems. The system was designed with intrinsically safe control circuitry intermingled with 120-V ac pow- er in a multiconductor control cable. To remedy this situation, 480- to 120-V ac transformers were installed into each motor control box and additional safe isolation relays were installed. The main contactor allowed 120-V ac power in- to each control box even when the main switch was in the "off" position; this was corrected by replacing the original contactor in the master control box with a circuit breaker located in a separate enclosure. The changes made to meet MSHA requirements are listed in appendix A. PLANS Based upon observations made during surface testing, the following mine re- quirements are suggested: • The minimum working height of the MBC is 48 in. The minimum working height increases to 54 in if the outby end of the MBC is supoprted by a 6-in high low- belt structure (figs. 24-25). Additional working clearance would ease cleanup un- der the MBC. • Maximum gradability of the system is 6.5 pet without excessive tram motor wear. Greater grades can be negotiated at the expense of decreased tram-motor life. • A minimum entry width of 14 ft is possible if 60° crosscuts are used and intersection corners are rounded; how- ever, a wider entry is desirable to allow a walkway at all points on the clearance (right) side of the system. Roof bolt (typical load 2,0001b) hanger FIGURE 24. — Monorail installation with chain hangers. 25 4" reference Outbyunit control box 54 M min .5-hp Monorail track -^ ■•— | n by tram motor Belt direction — Drawbar Main power cable T 8" reference Power and control cables to other units Low-belt structure Belt direction -»► (panel belt) FIGURE 25.— Monorail installation with roof plates over low-belt structure. 60° SIMPLE CURVE System con be used ; _ 29° angle between A~B and BC is <40° NOTES: Maximum angle between units is 40°, Only RH turnouts are shown. Angle of switches, 11°. Arc of track sections: MK-3 and MK-5, 12°; MK-4, 24°; MK-7, 19°; andMK-8,3l°. (MK-7andMK-8 track not available at time of tests.) All track curves on 24- ft radiurs. All track is shown centered in 18-ft entry. _1 *^o Crib or post -»Q *G 90° SIMPLE CURVE System cannot be used; 49° angle between AB and BC is > 40° 90° COMPOUND CURVE System can be used; 34° angle between BC and C~D is <40°. However, 2 x FH=2 x 39ft=78ft. This is too wide. Mine would require extra roof support so that 2 x GH <70ft. KEY ■ Splice plate MK-5 Track designation AB Represent units (each 24-ft long) PT Point of tangency FIGURE 26.— Monorail bridge conveyor track turnout plans. 26 • The MBC was designed for 60° cross- cuts using the 24-ft radius monorail track, however, crosscuts of 90° can be negotiated using a compound curve. In any turnout configuration, the angle be- tween MBC units must be less than 34° to prevent unit-frame interference with each other. An advantage of 60° crosscuts is that spillage between units will be minimized because potential spillage at transfer points increases as the angle between units increases. Figure 26 shows track installation plans for both 60° and 90° crosscuts. • Suporting the MBC system should not be a problem because the eight-wheel car- riers distribute conveyor weight over a 6-ft length of monorail track, which re- sults in a typical load on each suspen- sion point of less than 1 st. Although not tested, resin bolts are recommended over mechanical bolts to better withstand tramming-induced vibration. The MBC can be used for room-and-pillar mining (figs. 27-29), longwall develop- ment (fig. 30), or shortwall mining (fig. 31). For room-and-pillar mine plans, the monorail track does not have to be in- stalled in all mine entries. As illus- trated in figure 27, the monorail track would typically be installed over or beside the panel belt in the center en- try and in each crosscut. The combined length of the inby MBC unit and the con- tinuous miner enables raining in entries that do not have monorail track in- stalled. The hopper of the inby MBC unit can be up to 20 ft from the last point of monorail suspension. Assuming that a typical continuous miner is 35 ft long, the continuous miner cutterhead can be up to 55 ft from the last point of mono- rail installation (fig. 32). Various cut plans are possible, depending on local conditions. Continuous miner HFB surge car 1 2-unit system Monorail track FIGURE 27.— Five-entry mine plan. 27 FIGURE 28.— Five-entry 60° mine plan with rooms. M 5 | 12 10 23 26 24 22 20 16 1a 27 29 31 ^>K ■ I LEGEND [7] Cut number 32 35 37 40 E*lE M 1 l 1 1 1 > 1 » 1 * 1 1 H * l 1 v !y 1 . 1 1 . 39 41 M3 45 J--75- •J < t I » 1 1 ' 1 1 in 1 1 1 1 1 1 1 1 1 n 1 1 ^ ■ «^ ^| l| >immm 1 > ■ t > 1 « » » i I I M I I I > » » I t ■ < t * ) I » I I » ■ I I I I M l I MM Ml IM I i l M -18' Return Intake Intake Be FIGURE 29.— Seven-entry mine plan t Track Intake Return (power) 28 Panel belt MBC system Monorail track Belt Intake Return 60° (typical) FIGURE 30.— Mine plan for longwall panel-entry development. mm mm -r-Panel belt conveyor :}:<~rj:!: MBC system Continuous miner mm ml Jr.- "I ^_J : ' ,■„ ' . ' : ' ? . 9 l t . ' ■■..■ - ■-. ! „ Chock FIGURE 31.— Monorail bridge conveyor used with shortwall mining system. ■fSKAtt* A potential application of the MBC sys- tem would be in longwall panel develop- ment. As shown in figure 30, the 288-ft MBC system would be of sufficient length to advance two crosscuts of a three-entry heading, thereby potentially reducing longwall-panel development time. An alternate use of the MBC system would be to provide continuous haulage capability for shortwall raining sec- tions. Shortwall raining has the poten- tial to provide productivity advantages of longwall raining without high capital costs. A major impediment to more short- wall application is the lack of a contin- uous haulage system. As shown in figure 31, the MBC connects the continuous miner to the panel-belt conveyor with the mono- rail track bolted to mine roof in the headgate entry. In the face area, the monorail is supported underneath chocks with the provision that the lightweight monorail track could be manually con- nected after the chocks are advanced. 29 rf5L.-L -„ 7 I^=m^m//=//7rm/r//i^/////L 55' FIGURE 32.— Monorail bridge conveyor with continuous miner. FIGURE 33.— Hopper-feeder-bolter. If oversize material (over 12 in) is regularly encountered during the mining cycle, a crusher should be used inby the MBC system to avoid clogging MBC trans- fer points. The previously described HFB with optional bolter removed, shown in figure 33, can perform that task. Additional advantages of using the HFB between the continuous miner and MBC are that (1) surge capacity is provided; (2) an outby feeder breaker can be elimi- nated; and (3) extra system reach is pro- vided. As seen in figure 34, the contin- uous miner cutterhead can be up to 80 ft from the last point of monorail installa- tion. If the MBC is used with the HFB, the two systems could be connected (fig. 35). 30 Miner operator Hopper feeder operator Miner- feeder cable handler 50 ft* lb). Less than 20 ft* lb of effort was required with the solid tire. Nov. A steering motor, gearbox, and re- 1982 mote steering-control circuit were installed for the inby tram drive. Nov. Isolation relays to provide in- 1982 trinsically safe circuits were added to the tram and steering controls. The original manual steering was undesir- able because it was difficult to operate, and it put the operator in an unsafe position. Intrinsically safe circuits were required to enable use of nonexplosionproof limit switches and pendant control. Nov. Grease fittings were added to the 1982 conveyor drive couplers. Nov. The spacing between the conveyor 1982 return roller for the belt- sequence switch and the conveyor return roller for the belt-slip switch was increased from 24 to 48 in. Additional lubrication was required to prevent frequent coupler disengagement. The original, closely spaced, return rollers were not turned by the belt dur- ing loading trials, because increased belt tension caused the belt to lift from the rollers. Nov. A 3/16-in/ft crown taper was added Belt-alignment problems were experienced 1982 to the head and tail rollers. during coal loading trials. Crown taper tends to self-center the conveyor belt. Dec. Adjustable hoop-type angle deflec- 1982 tors were added on the outby end of each unit. Deflectors were required to center the coal transfer to minimize spillage. The hoop-type deflectors were required to prevent coal from hitting the suspension yoke when two units were at an angle. 33 MODIFICATIONS TO THE MONORAIL BRIDGE CONVEYOR SYSTEM— Continued Date Modifications Reason Dec. 1982 Jan. 1983 The profile of the suspension yoke The original suspension yoke was struck by was modified to allow a greater coal when units were at their raaxiraum- opening for coal transfer. angle relationship. Compression-spring-type belt cleaners were installed under- neath the head roller. Belt cleaners were required because coal tended to accumulate on the underside of the conveyor belting, causing belt mis- alignment and opening of the slip switch. Jan. A lightweight pendant control was 1983 installed. June The wheel base between the 9-in- 1983 wide inby rubber tires was in- creased from 12-in centers to 38-in centers. Originally, an explosionproof control unit was installed. This heavy unit was awk- ward to use and only had controls for conveying and tramming. Extra controls were required because a steering motor was previously added. Tramming tests proved that the inby unit was unstable with original close-wheel base. Stability is required to prevent belt misalignment. June The inby tram drive was changed to 1983 a gear-speed reducer mounted be- tween the inby rubber tires. June Limit switches were installed to 1983 limit the allowable steering arc of the inby wheel carriage. The original chain and sprocket drive was unreliable and had poor ground clearance. Without limit switches, the wheel carriage turned until stopped by mechanical inter- ference. This in turn would overload the steering motor. June A limit switch was installed to 1983 detect when the inby monorail carrier reached the end of the monorail track. Aug. A heavier inby tram-motor torque 1984 arm was anchored to both sides of the through-bolts on the inby tram-speed reducer. Aug. Cast bearings were installed to 1984 support the steering shaft. This switch prevents the monorail carrier from tramming off the inby end of the monorail track, thereby avoiding a possi- ble safety hazard and operational delay. The original torque arm was only attached to one side of the speed reducer, and it failed during tramming tests. The original pressed bearings did not resist the lateral thrust produced by the steering shaft. This caused the steering-shaft key to disengage from the drive coupler. Nov. The inby tram drive was changed 1984 from two- to one-wheel drive. The original design with both wheels mounted on a solid shaft required exces- sive torque requirements for steering, since the wheels would slide instead of roll during steering maneuvers. 34 MODIFICATIONS TO THE MONORAIL BRIDGE CONVEYOR SYSTEM — Continued Date Nov. 1984 Dec. 1984 Feb. 1985 Modifications A brake was added to tbe steering motor. Reason The brake was required to lock the steer- ing carriage when the steering motor was not in operation. A new explosionproof steering con- The control box was required for steering trol box was installed on the controls, inby unit. A 5/16-in-thick MSHA-approved PVC The original, 3/16-in-thick belt was not conveyor belting was installed in adequate for underground use. all units. Feb. 1985 Feb. 1985 Several 4-in-diam clearance holes were burned into the conveyor frame to allow better access to the conveyor drive coupler. The original 1.5-in-diara hole made coupler adjustment difficult. Gussets were added to the sides of The switch mounting frames would be prone the sequence and slip-switch to damage during MBC installation because mounting frame. they extended below the main conveyor frame. Mar. The 480-V ac to 120-V ac trans- 1985 formers were installed into each motor control box to power system controls. Mar. Isolation relays to provide in- 1985 trinsically safe sequence-switch circuits were installed into each control box. Modification was required to meet MSHA re- quirements. Originally, 120-V ac control power for all units was supplied by one transformer in the master control box; however, this 120-V ac power was inter- mingled with intrinsically safe control wiring in a multiconductor cable. Modification was required to meet MSHA requirements. Previously, the 120-V ac sequence-switch circuits were inter- mingled in the multiconductor cable with intrinsically safe circuits. Mar. The brake overhead indicator lamps These items were removed to provide space 1985 and associated relays were re- for the transformer and isolation relays moved from each motor control box. Mar. A 480-V ac to 120-V ac and 12-V ac The 120-V ac power was required for steer- 1985 dual secondary transformer was ing control, and 12-V ac power was re- added to the steering control quired for lighting, box. 35 Date MODIFICATIONS TO THE MONORAIL BRIDGE CONVEYOR SYSTEM— Continued Modifications Reason Mar. A main circuit breaker explosion- 1985 proof control box was added to the MBC control system. Modification was required to meet MSHA re- quirements. Previously, the contactor in the master control was the main circuit- interrupting device; however, with the contactor, there was 120-V ac power in all units, even when the main power switch was in the "off" position. A new main breaker box was required be- cause the existing master control box did not have an opening for a circuit- breaker reset handle. Mar. Fuses were removed from the line 1985 side of the 480-V ac transformer in the master control box. If the fuses were left in, the master con- trol box would require a panel-interlock switch. Mar. The ground-monitor circuit was 1985 removed from the master control box. The circuit would be redundant with the load-center ground-monitor circuit. Mar. An explosionproof junction box was 1985 added on the inby unit so that both headlights could receive power from one cable exiting the steering control box. Mar. An explosionproof junction box was 1985 added to the outby unit so that both taillights could receive power from one cable exiting the master control. An extra cable-entrance gland was required in the steering control box for the steering control brake. An extra cable-entrance gland was required in the master control box for the main- breaker shunt-trip cable. Apr. All interconnecting cables were 1985 placed in MSHA-approved flame- resistant hose conduit. Modification was required to meet MSHA requirements. June New cable hangers were installed 1985 on all units. The new cable han- gers acted as trays and could hold several cables. Previously, separate cable hangers were installed for each interconnecting cable. This made adjustments awkward. June Tapped mounting bosses were in- 1985 stalled on the inby end of each unit. The mountings were required to permit rapid attachment of a changeout bracket. The bracket is connected to a monorail- suspended chain hoist when unit changeout is required. 688 365 U.S. GOVERNMENT PRINTING OFFICE: 1987 605-01 7'60 070 INT.-BU.OF MINES,PGH.,PA. 28526 U.S. Department of the Interior Bureau of Mines— Prod, end Distr. Cochrane Mill Roed P.O. Box 18070 Pittsburgh. Pa. 15236 OFFICIALflUSINESS PENALTY FOR PRIVATE USt MOO [ J Do not wi sh to recei ve thi s material, please remove from your mailing list* | "l Address change* Please correct as indicated* AN EQUAL OPPORTUNITY EMPLOYER X 1T % • ^^ ~^ x»y v **- < ^r^ + ^ x *>^X «> ^ \ < ^P*v n i X *y%$>/ j? X *&%m*s X x. •> ^°- Jfc*. ^ * '* %,£,,•„ *^ 1 vrV «5» ^ %^ :£& ^ %,■? <- ,•1°* v xv .•■ "V .»p* .«••*% v.££&\ ,** •>. '•-^% /^A c .^* y.-^k-V o°%^> /S - ■>„ g°* y;^ °o ,** ^^ ^ 0^ »-' 1 A V "^ a v *^ : PHi^ c^^ °^ / %•••:«:.•♦ \--^-/ v : " ; *>*' %" : ^^ , > v ' X «»i. 'oK 6^ °?0 X/' -«fe \y • oN °» *^ O *'V. * 4 «G V O *».»* -A ^b A> V 0°"°-. **ft .% ^ 6 V ^ »* .<& \ r *^^* . ^' .^^ ^ 4V »!» o. * VV ■5*r ^•0 ^ a> S^mtsT* ^o tA V ^. • ^.^^ :'£MP'^\ '^,